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Diffstat (limited to 'target/linux/brcm2708/patches-4.14/950-0285-Reduce-log-spam-when-mailbox-call-not-implemented.patch')
-rw-r--r--target/linux/brcm2708/patches-4.14/950-0285-Reduce-log-spam-when-mailbox-call-not-implemented.patch78
1 files changed, 0 insertions, 78 deletions
diff --git a/target/linux/brcm2708/patches-4.14/950-0285-Reduce-log-spam-when-mailbox-call-not-implemented.patch b/target/linux/brcm2708/patches-4.14/950-0285-Reduce-log-spam-when-mailbox-call-not-implemented.patch
deleted file mode 100644
index 0377aac2da..0000000000
--- a/target/linux/brcm2708/patches-4.14/950-0285-Reduce-log-spam-when-mailbox-call-not-implemented.patch
+++ /dev/null
@@ -1,78 +0,0 @@
-From 785c44fa278b7dd7a4b96c64321dc43fa2220f7d Mon Sep 17 00:00:00 2001
-From: James Hughes <james.hughes@raspberrypi.org>
-Date: Fri, 27 Apr 2018 10:13:35 +0100
-Subject: [PATCH 285/454] Reduce log spam when mailbox call not implemented
-
-This changes the logging message when a mailbox call
-fails to the dev_dbg level. In addition, it fixes the
-low voltage detection logging code so that if the
-mailbox call doies fails, it logs at error level
-and flags so the call is no longer attempted.
-
-Signed-off-by: James Hughes <james.hughes@raspberrypi.org>
----
- drivers/firmware/raspberrypi.c | 23 ++++++++++++++++++-----
- 1 file changed, 18 insertions(+), 5 deletions(-)
-
---- a/drivers/firmware/raspberrypi.c
-+++ b/drivers/firmware/raspberrypi.c
-@@ -151,7 +151,7 @@ int rpi_firmware_property_list(struct rp
- * error, if there were multiple tags in the request.
- * But single-tag is the most common, so go with it.
- */
-- dev_err(fw->cl.dev, "Request 0x%08x returned status 0x%08x\n",
-+ dev_dbg(fw->cl.dev, "Request 0x%08x returned status 0x%08x\n",
- buf[2], buf[1]);
- ret = -EINVAL;
- }
-@@ -204,6 +204,7 @@ EXPORT_SYMBOL_GPL(rpi_firmware_property)
-
- static int rpi_firmware_get_throttled(struct rpi_firmware *fw, u32 *value)
- {
-+ static int old_firmware;
- static ktime_t old_timestamp;
- static u32 old_value;
- u32 new_sticky, old_sticky, new_uv, old_uv;
-@@ -214,6 +215,9 @@ static int rpi_firmware_get_throttled(st
- if (!fw)
- return -EBUSY;
-
-+ if (old_firmware)
-+ return -EINVAL;
-+
- /*
- * We can't run faster than the sticky shift (100ms) since we get
- * flipping in the sticky bits that are cleared.
-@@ -232,8 +236,17 @@ static int rpi_firmware_get_throttled(st
-
- ret = rpi_firmware_property(fw, RPI_FIRMWARE_GET_THROTTLED,
- value, sizeof(*value));
-- if (ret)
-+
-+ if (ret) {
-+ /* If the mailbox call fails once, then it will continue to
-+ * fail in the future, so no point in continuing to call it
-+ * Usual failure reason is older firmware
-+ */
-+ old_firmware = 1;
-+ dev_err(fw->cl.dev, "Get Throttled mailbox call failed");
-+
- return ret;
-+ }
-
- new_sticky = *value >> 16;
- old_sticky = old_value >> 16;
-@@ -270,10 +283,10 @@ static void get_throttled_poll(struct wo
- int ret;
-
- ret = rpi_firmware_get_throttled(fw, &dummy);
-- if (ret)
-- pr_debug("%s: Failed to read value (%d)", __func__, ret);
-
-- schedule_delayed_work(&fw->get_throttled_poll_work, 2 * HZ);
-+ /* Only reschedule if we are getting valid responses */
-+ if (!ret)
-+ schedule_delayed_work(&fw->get_throttled_poll_work, 2 * HZ);
- }
-
- static ssize_t get_throttled_show(struct device *dev,